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- 2007 Spring Meeting & 3rd Global Congress on Process Safety
- Ethylene Producers Conference
- Ethylene Fundamentals and Technology
- (52a) Revamp of Pygas Unit to Meet New Sulfur Regulation
The implementation of this project has yielded the following demonstrated key performance indicator (KPI) improvements:
· C7+ pyrolysis gasoline sulfur content reduced from 300 ppmw to less than 3 ppmw. · Styrene conversion increased in the first stage reactor system from ~75% to more than 95% · Lower Weighted Average Bed Temperature (WABT), extended cycle time · Fouling and pressure drop build-up mitigated in the first stage reactors · Elimination of frequent catalyst regenerations, resulting in a significant decrease in plant workload, associated expenditures, and exposure of personnel to the process
Over 230 hydroprocessing units, including several pygas applications, have demonstrated the value of Shell Global Solution's ?know how? and reactor technology. This paper highlights performance improvements that have been commercially demonstrated in a pyrolysis gasoline application when operating and design ?know how? and cutting edge technology are integrated into a low cost revamp solution.