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- (389b) Mixing Scale-up for An Air Oxidation Process
Sabic worked with an agitator vendor to perform scale-up trials for an agitator design for reactors to be installed as part of an air oxidation process. Reactions had previously been performed at a 2-liter lab scale and also at a 1m3 pilot plant scale to finalize the reaction conditions and procedure. The agitation trials were necessary to finalize the details of the agitator and baffling for the 23m3 commercial reactors. A preliminary design for the reactor cooling coils had been developed and the agitation trials were also designed to confirm the adequacy of that design, considering the overall heat transfer coefficient as well as the effect of the coils on the vessel agitation.
Agitation trials were carried out utilizing a clear plastic vessel, 1 m in diameter by approximately 1.5 m straight side height. Geometric similarity was maintained with the proposed design. Two concentric sets of cooling coils (1” OD x 9 wraps each) were installed, along with a 5% baffle located between the two sets of coils. Two stages of impellers (0.45m in dia.) were provided, a radial flow impeller close to the lower tangent line of the vessel and near the point of introduction of the air, and a combination radial/axial flow impeller located 0.45m above the lower impeller. A sparge pipe was provided to inject air just under the lower impeller. Water was utilized as the agitated fluid, and the top of the vessel was open to facilitate insertion of baffles, piping, and instrumentation and for visual observation of the quality of agitation. Compressed air was provided, along with flow control, to allow study of the agitation under varying degrees of aeration. Scaling of the airflow was done to compensate for the operating pressure and temperature differences between the ambient atmospheric agitation trials and the commercial reactor. This scaling was done in order to more closely duplicate the gas void fraction that would be experienced in the commercial reactor. The scale of the trial reactor was 1:2.8 in length (1:22 in volume) compared with the commercial reactor, and the geometric scaling was preserved within 5% on critical dimensions. Agitator rotational speeds of 0 to 230 RPM corresponded to 0 to 110 RPM on the commercial reactor, considering equal power per unit volume.
Following is the list of studies performed during the agitation studies:
Results from the agitation trials were used to finalize the details of the agitator, baffling, and the cooling coil design for the commercial reactors.
After installation of the plant reactors, and before plant start-up, water runs were conducted as a part of plant commissioning. Mixing trials were conducted at various agitator speeds and airflows to determine the flooding point. This was necessary in order to set the minimum recommended agitator speed that would insure adequate gas-liquid contact and avoid “bypassing” of un-reacted oxygen directly to the reactor headspace. This was important for conservation of air as well as being one of several measures necessary for the avoidance of flammable mixtures in the reactor headspace.
During the plant commissioning some of the U-bolts used to attach the cooling coils to their supports were found to be fatiguing to the point of failure. A finite element analysis indicated that the coil supports needed to be improved in order to increase the stability of the coils against vibration under agitation conditions to avoid fatigue and failure of the U-bolts. Insufficient communication between the vessel manufacturer and the agitator supplier regarding the stresses induced on the coils by the agitated fluid led to the under design, illustrating a critical communication that needs to take place during the design phase for agitated vessels with complex internals. Redesign of the supporting brackets and U-bolts, based on the findings of the finite element analysis, led to an installation that has been successfully operated with no further fatigue related issues.
After start-up of the oxidation reactors, data were taken to determine the actual heat transfer, and the available heat transfer was compared with the required heat transfer and that predicted by the correlations developed during the agitation trials. Observations were also made regarding the concentration of oxygen in the reactor headspace and the implications regarding the quality of the agitation vs. that required by the reaction and mass transfer rates.